The Locomotive
Modest in size, a large number of locomotives similar to Rx207 were
introduced from 1886 to haul goods trains over the heavily graded sections
of the Intercolonial Railway with up to 3 locomotives being used to haul
the Adelaide to Melbourne Express. They outlasted the large power locomotives
introduced in the 1920s as their replacement on main line trains, and they
were still being used on branch line trains and as shunt engines up to the
demise of steam in the late 1960s.
The Restoration
SteamRanger rescued the loco from the scrapper’s torch in the late 1960s
and operated it on enthusiast and tourist trains for many years on lines
round the State including many years on Cockle Train duties. By 1996 many
of its major components were worn to such an extent that an almost total
restoration was essential.
The work was progressively undertaken by SteamRanger’s two employees and
twenty or so dedicated volunteers. For a locomotive designed in the 1880s
and built in 1913, replacement parts were not readily available and the
knowledge and expertise on locomotive restoration was hard to come by.
Consequently, the only option was to manufacture many of the required
replacement parts in SteamRanger’s own workshops.
Old repair techniques
were analysed and, where appropriate, today’s more modern technology
adapted to aid the restoration process. Restoration proceeded whilst
SteamRanger continued to operate its regularly scheduled services.
There were many frustrating times when finances were tight and effort
was required on other projects.
Ian Johnston's photo on the right shows the starting point of the
restoration - the frame and wheels separated from the body, boiler
and firebox. His photos below illustrate just some of
the ensuing activities involed in this massive task
Ron Williams and Brian Wood machining piston rings
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Inside the firebox, Kim Critchley cleaning boiler tube holes
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Back together again - the frame and wheels reunited!
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And the refurbished boiler goes outside for testing
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Nearly there! - the boiler reunited with the frame and motion
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2011 Update
After returning to service in late 2001 the loco operated regular Cockle Train and other services until 2007 when it was again withdrawn to allow a major reconditioning involving both the boiler and motion. The loco was returned again to service in March 2011. Details of this project have been reported elsewhere on this website.
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